Official Mt.Madonna Thread!
Registered User
iTrader: (11)
Joined: Nov 2010
Posts: 2,196
From: Morgan Hill
Car Info: 2011 WRX Sedan
I was just driving my car (2011 wrx, catless dp, perrin exhaust, forge bpv, perrin tmic with torqued performance stage 2 tune) and went to pass someone on the freeway at about 60-70% throttle after building boost for a matter of a few milliseconds my car stop pulling and slowed down and i heard a banging sound (i felt as if my tmic had came unbolted and smacked against my hood to try and explain the sound) then milliseconds later my CEl light came on and the car began to pull again but of course i let off completely. The CEL remained on for the rest of my 5 mile drive. I got to work and popped the hood and everything looked and sounded fine so i turned off the car and turned it back on again with the CEL. Any idea what the *&^$ just happened?
Note* I just installed the TMIC yesterday and had sent in two 3rd gear pulls to Eric who then returned with a new map (still stage 2 tuned).
Note* I just installed the TMIC yesterday and had sent in two 3rd gear pulls to Eric who then returned with a new map (still stage 2 tuned).
General Pimpin'
iTrader: (7)
Joined: May 2003
Posts: 23,019
From: Knee deep in beer. subabrew crew, ca.
Car Info: MY04 aspen wrx wagon.
stock intercooler? How much boost?
I'd recheck the intercooler hoses first. More than likely one of those popped off. But those intercoolers can blow at the seems. I think Heedz might have had trouble with that on his legacy.
What code? I have a reader but I won't be out that way until Wed.
I'd recheck the intercooler hoses first. More than likely one of those popped off. But those intercoolers can blow at the seems. I think Heedz might have had trouble with that on his legacy.
What code? I have a reader but I won't be out that way until Wed.
Registered User
iTrader: (11)
Joined: Nov 2010
Posts: 2,196
From: Morgan Hill
Car Info: 2011 WRX Sedan
stock intercooler? How much boost?
I'd recheck the intercooler hoses first. More than likely one of those popped off. But those intercoolers can blow at the seems. I think Heedz might have had trouble with that on his legacy.
What code? I have a reader but I won't be out that way until Wed.
I'd recheck the intercooler hoses first. More than likely one of those popped off. But those intercoolers can blow at the seems. I think Heedz might have had trouble with that on his legacy.
What code? I have a reader but I won't be out that way until Wed.
The tune should be 19 but my ap said it boosted 21...
General Pimpin'
iTrader: (7)
Joined: May 2003
Posts: 23,019
From: Knee deep in beer. subabrew crew, ca.
Car Info: MY04 aspen wrx wagon.
Yeah Heedz got that intercooler to solve a tmic issue. So my guess is something is loose in there or a hose came off.
Have you been retuned with the TMIC?
Pretty common for a house to not get on just right during an install. Those things suck to put on.
Have you been retuned with the TMIC?
Pretty common for a house to not get on just right during an install. Those things suck to put on.
Registered User
iTrader: (11)
Joined: Nov 2010
Posts: 2,196
From: Morgan Hill
Car Info: 2011 WRX Sedan
Cool ill do it on my lunch break.
Idk man i got that hose pretty damn tight...how bad is it to drive on for a few miles? I dont have time to fix it until i get home, about 3 miles...
Idk man i got that hose pretty damn tight...how bad is it to drive on for a few miles? I dont have time to fix it until i get home, about 3 miles...
Registered User
iTrader: (12)
Joined: Sep 2011
Posts: 2,057
From: San Mateo, CA
Car Info: 2015 FXT Stage II
Brenden it's one of two things you either overboosted or the throttle body hose slipped off its a known issue on our car. The throttle body hose is my bet though. You have a CEL right? Check the code on the access port and post what it says.
Just saw you said 21psi that's way too high tell Eric to adjust your WGDC because you are over boosting.
Just saw you said 21psi that's way too high tell Eric to adjust your WGDC because you are over boosting.
Registered User
iTrader: (12)
Joined: Sep 2011
Posts: 2,057
From: San Mateo, CA
Car Info: 2015 FXT Stage II
Originally Posted by bkblitzed
Boosting at 22psi is awesome though lol. I missed boosting that high
Boosting above 20 on pump isn't too safe. Brenden don't go WOT anymore over boosting isn't that great
General Pimpin'
iTrader: (7)
Joined: May 2003
Posts: 23,019
From: Knee deep in beer. subabrew crew, ca.
Car Info: MY04 aspen wrx wagon.
Brenden it's one of two things you either overboosted or the throttle body hose slipped off its a known issue on our car. The throttle body hose is my bet though. You have a CEL right? Check the code on the access port and post what it says.
Just saw you said 21psi that's way too high tell Eric to adjust your WGDC because you are over boosting.
Just saw you said 21psi that's way too high tell Eric to adjust your WGDC because you are over boosting.
General Pimpin'
iTrader: (7)
Joined: May 2003
Posts: 23,019
From: Knee deep in beer. subabrew crew, ca.
Car Info: MY04 aspen wrx wagon.


